Shake down report... Please let me start this off by 1st saying this... "IN YOUR FACE HOSER!!!" The front end modification that he was so critical about worked great... Still have some push but this was due to the rear end not having a differential...the suspension worked perfect, soaked up ruts, washouts, jumps and without wanting to jerk the controls out of my hands. In a stock Pilot, the steering gets sensitive at speed...not the case now, it smoothed out more as speed increased and wanted to track straight and not try to grab directions...at one point I was driving 1 handed with no problems...The different geometry of the Kawasaki front end and the addition of the GPR was the nats ass. To the guys that manufacture the LT suspension for these, junk the stock Honda hubs and go with the Kaw KFX700 hubs. This gives you disc brakes, uses the same tie-rod ends and has a different throw point for the tie-rod at the hub. I did add the GPR but had it set at it's lowest setting and it was more than enough...
Steering...still have some push but found by gasing the rear around, it could still turn fairly sharp...more weight in the front would help but at this point, not sure what I could shift forward and I don't want to add weight just to add weight...
Engine temp... Water temp never went about 190 and the fan wasn't kicking on....today was about perfect for temps, 80 outside temp today... This could change though with some jetting.
Now for what to change...need to re-jet. I have it close by the plug but it's still a little rich. Going to lean it out and drop down one more size on the main...It was starting out good but would bog down a little at mid range...I'm not the best at jetting so I have a friend who has driven 2 stroke motors for years. I also have to get more power for the lights...Anyone know of a high output stator for the FL400R? I bumped the light switches on and they drained the battery within 20 minutes...once I found out the problem, a turned the switches off, gave the pull starter a good pull and I was back on the track...Until I find a new stator, going to install a master power switch for all the extras...manage the power a little better. Finally the thumb throttle is really stiff...has good spring response so going to look for a lighter spring...
Overall I am very pleased with the results of the modifications...The aluminum body is going on, take it to the races this weekend for a good shake down run...barring any problems, Monday it will get stripped down and sent off for powder coat and the body will get some graphics for my sponsors...
I did shoot some video but I had MX helmet on with the visor and it kept hitting the camera...still cool video but it changed the shot so you couldn't see the controls...I'm adding some additional mounts for the Go-Pro. The suspension was very smooth and having it mounted to cage it really showed how smooth and how well the suspension worked.